Wednesday, December 28, 2011

Sunbeam S7 / S8 permanent magnet alternator conversion (recap)

This is a recap of my alternator build.
(as published in the Sunbeam Owners Fellowship club magazine "On The Beam" issue Nov-Dec 2011)



I’ve been frustrated with the original Lucas dynamo on my Sunbeam since I’ve been riding it. Neither the MC45O nor the MC45L (that I later purchased) produced enough electricity in a foolproof fashion. I don’t want to have to worry about if there’s enough charge in the battery to get me home anymore, and I want to run the lights all the time. I also don’t want an after-market alternator conversion that does not look exactly like the original. This is why I was determined to create an alternator conversion by myself for a small price. I submit the following to any interested do-it-yourself owners.
I took suggestion from some Douglas and Vincent motorcycle owners who also have problems with dynamos. A few intrepid owners have taken permanent magnet alternators from modern applications and fit them inside the original dynamo cases. One particular application caught my eye while searching online for a suitable solution. There is a simple alternator from a Kubota tractor that measures only 3-1/2” across and a little over 3” high. I bought model APM0001, which was the smallest available. This came as a self-contained belt driven assembly. I tested it briefly before taking it apart to see how easily it produced enough current being turned by hand to light the tail lamp bulb on my bike. Removing the nut and pushing the bolt out easily disassembled the unit, shown in Figure 1. The back housing was discarded.

Figure1

The magnet cup was surprisingly powerful. It all fit nicely into the original dynamo case. There would be two major challenges. Fit the magnet cup to the crankshaft, and then to fit the case back onto the engine block so it all stayed together. I elected to do the reverse of what the Douglas owners had done, and fit the magnet cup onto the shaft first, so that the stator would be accessible from the front of the bike. It sounded wrong at first, but it eliminated so many problems it was worth the effort, in my mind, to machine all the required parts on the lathe. There would have to be an adapter to fit to the end of the crankshaft, which included pins to fix the magnet from rotating independently from the crankshaft. This I spun out of round stock on the lathe to a relatively high degree of precision. I would use the original left-handed bolt so I didn’t have to machine another one. The outside casing would have to be secured to the engine block by means other than the two long bolts originally used, because they interfered with the outside diameter of the magnet. The wires could easily come out the front and affix to the original terminal block. Below is the solution showing the framework cage that was made to hold the outside casing. I could have welded tabs to the casing, but I didn’t want to modify it.
Figure 2

The whole assembly fits together with a specific procedure, it’s not ideal, but it works. (I later discovered that the magnet was so strong, that I needed to fit two of the sealed bearings inside the stator winding assembly to keep it centered with respect to the crankshaft. That isn’t represented in the photographs.)

The cage, at the left of Figure 2, goes on first. The magnet and center bolt (with spacer) then affix to the crankshaft adapter. The spacer holds the sealed bearings from the original Kubota unit, and another outside press-fit spacer makes up the difference between the stator and the outside bearing race.  The fourth arm of the cage assembly encloses the magnet, before the case is slid onto the cage. The pole shoe screws fasten the case to the cage in such a way that it forces the case into the engine block firmly as the countersunk screws are tightened. The stator coil, at the right side of Figure 2, slides into the magnet which is centered by one of the bearings from the original alternator assembly. This took a brass spacer precisely machined out of an old pipe fitting. The wires tuck neatly up against the casing out of the way of the rotating magnet. The outer plate bolts on with 6 screws and then the cast aluminum cover of the dynamo bolts to the outside of the case.




Figure 3

I’m quite pleased that the mechanics of my alternator conversion work well. The next challenge was to rectify and regulate the alternating current into direct current. Normal people would just have converted to 12 volts and put the Kubota tractor regulator in place of the Lucas MCR2 dynamo regulator. I had purchased a Rooster Booster 6 volt positive ground ignition module, and already had my 6 volt battery and lamps, so I was determined to stay with 6 volts for the present time. I know it’s not ideal, but I knew I could make it work fine. The 6 volt scooter rectifier/regulator that I bought was quickly overwhelmed by the 14 amp capacity (and probably the open circuit voltage capability) of the stator coil, and burned out. I ended up with a commercial shunt regulator from Electrex World LTD.

I spent a lot of time on this project, but it met my goals. It looks original from the outside, it is reliable, and it was less expensive than the alternatives, as long as I don't count my massive investment of time.

Keep Shafting

Saturday, December 3, 2011

Truck-Lite headlamp evaluation

I've been given a Truck-Lite model 27250C for evaluation.  It is an Light Emitting Diode -based drop in replacement for a 12 volt standard 7" headlamp with high and low beam.  Since there's only one, I've installed in in my XS650.


Initial indication is that the beam pattern is a bit strange.  The beam is strongest in a small square in the center, with a wide pattern without much vertical dispersion.  Looking into the lamp is absolutely dazzling.

This first photo is the low beam setting compared to the beam cast by the single 3 Watt Luxeon LED installed in the Sunbeam S7.  There's a big difference in intensity.  The single Luxeon is feeble in comparison.

This second photo is the high beam setting on the Truck-Lite headlamp.  (The single Luxeon was turned off in this photo).  There's not tremendous difference as captured by the camera, but in person it is a very intense light.  The brightest part is very focused, and the dispersion away from that point is rather poor giving very intense light only at that specific point.  Ride to work on Monday morning should provide the practical nature of this LED headlamp.
More later....

Sunday, August 21, 2011

Voltage Regulation

... or lack of voltage regulation as the case is.  The alternator actually works too well.  I bought this cheap regulator/rectifier intended for scooters.  Its voltage stability is horrendous.  Naturally the Permanent Magnet alternator increases in voltage and frequency as I rev the S7 Deluxe engine.  The regulator should compensate for this and keep the voltage around 6.x volts and not too high such as the 7.x volts that I saw this morning.  At highway revs the ammeter was reading nearly full scale of 8 amps!  "That's WAY TOO much current", I said to myself as I sat beside the road this morning.  The voltage kept going up with the revs... its supposed to be regulated to limit the voltage so that the battery won't get overcharged.  Well, the reason I was sitting beside the road this morning was that the battery WAS being overcharged and had blown the 7.5 Amp fuse that I had installed in series with it.  I was trundling along until I dropped the revs and the alternator wouldn't produce enough voltage to keep the ignition going... at which time the bike stopped running at the intersection.

A quick disconnection of the stator leads and a jumper across the fuse, limped KYL95 back home to the workshop.

So, now I need to replace that cheap scooter regulator.  I imagine its just a simple series pass transistor regulator in there, and its not yielding good results.  The correct solution is to use a switching regulator.  Like this one:

http://www.national.com/pf/LM/LM3150.html#Overview

Oh, and I've purchased a resettable circuit breaker too.  I HATE fuses.

Thursday, August 11, 2011

Alternator - First Test on bike Unregulated

I finished the construction of the frame that holds the dynamo case to the front of the engine. My buddy Mark was kind enough to do the welding. A few minor adjustments and some precision holes drilled and I was ready to fully assemble the alternator to the bike.



First the cage must be installed with one arm out.



Then the magnet cup can be installed and the center bolt attached to the crankshaft and torqued down.  The fourth arm is then installed.



The casing can be placed over the cage and the screws installed where the pole shoes used to be.  The critical alignment of the stator inside the magnet cup was done with extreme care and precise drilling.  The stator will have some larger screws holding it to the plate in the final assembly, and a spacer to make sure it stays parallel to the plate.



Everything gets tightened.  In the final assembly the wires would go to the stock terminal block, but for this test without the regulator, I'm just going to hook some jumper leads out through the front.



Old KYL95 started on the first kick and we had LIGHT!!!!!  The automobile headlamp provided some visual load.  The voltage was around 6 at tickover.  It increased to 12 if I revved it up a little.  The regulator/rectifier will be installed in the electrical box, after the cage is sandblasted and painted.

Friday, July 29, 2011

Alternator - Magnet fit to crankshaft

I finished the crankshaft adapter this evening and put the two anti-rotation pins in it.  The holes are tapped for 10-32 grub screws, and they are set in place with loctite.  I changed the design slightly while parting the adapter from the lathe.  It was easier to leave a 1/2" diameter raised ridge around the center of the adapter on the outside to allow perfect centering of the magnet cup, than creating a special washer for centering.  The bolt is 3/8" and the hole in the magnet cup is 1/2", so a method of getting it centered was required.  The run-out was acceptable, and I'm starting to think about creating the flange to hold the stator coil.  I still haven't decided on exactly what to make it from.  Aluminum would be easiest to machine, but I don't have a piece wide enough without having one cast to approximate shape.  I may make it in two parts and just bolt it together, but this becomes more challenging to keep it centered.  The original back piece of the Kubota alternator is too thick, but I might be able to machine it down.  The problem is that it still needs a wider plate to fasten to the edges of the housing.  The critical part will be to keep the stator perfectly centered, as not to touch the magnet.


I test fit the stator to check the magnetic center.  If I think the output is too high (since its designed for 12v output), I might be able to make the field strength adjustable by allowing the stator to pull out toward the front of the bike and weaken the magnet's grip.  I suppose I could use spacers or washers to accomplish this to get it just right when its all done.  It did light a 6 volt bulb readily only turning the alternator by hand. Hmmm.


I still need to make the inside frame for the housing so it can be fastened to the front of the engine, and give something to bolt the cover to.  That will be the next task.  One part of the frame inside the housing may need to be removable to install the magnet cup once the frame is in place.

Here's my buddy Mark testing out his plasma cutter and making some parts for the internal frame of the alternator.

Saturday, July 16, 2011

Alternator - The Build

From the last post, I've got pictures of the Kubota alternator all dismantled.  Next comes the modification pieces.

I've made an adapter ring plate to which flat bars will be welded to hold the case of the dynamo to the engine block.  This has the challenge of interference with the side of the case.  The cap screws that I will use will have to be ground down somewhat, and the side of the dynamo case ground down to accommodate the screws.  This should hold the case firmly to the engine block.



The next big item is machining the crankshaft adapter.  This will be a copy of the back of the armature, which will allow the magnet of the alternator to bolt directly to the crankshaft.  Here's a picture of it just started out of a piece of roundstock.  I'll need to get a parting tool for the lathe before I finish the part.



Here are the plans for the finished part.

Wednesday, July 6, 2011

Alternator - Proof of Concept

I'm fed up with the original Sunbeam S7 Lucas dynamo, and the MC45L dynamo that I bought. Neither one produces enough electricity in a foolproof fashion.
I don't want to have to worry about if there's enough battery to get me home anymore, and I want to run the lights all the time. I also don't want an after-market alternator conversion that does not look like the original.

The plan is to create an alternator conversion that produces 6 volts, is fully encased in the original housing, and works reliably.

I've seen others who have used a Kubota tractor permanent magnet alternator to do the job. Its only 3-1/2" in diameter and shorter than the MC45L dynamo. That means it should fit inside the casing. The trick is to mount it up.



It comes as a flange mount unit for belt drive, with its own bearings.

[edit]  I actually did use the bearings after all to keep the stator assembly centered in the magnet.  The magnetic forces are VERY strong radially, and will pull the stator into the magnet if there is the slightest mis-alignment or looseness.  A spacer piece was machined to hold two of the bearings into the stator and then the bearings were placed on the center bolt with their own machined spacers.

The permanent magnet rotor can attach directly to the S7 engine crankshaft, and the stator can mount to the engine block, or dynamo casing. All that is critical is that it runs centered and true. Should not be a problem for a guy with a lathe in his workshop.

Here's the sample fit up.  The center bolt presses out of the rotor cup easily.  This will allow me to make a bolt (left-handed Whitworth of course) to fit in there and mount to the crankshaft.  The question is whether 'tis better to bolt the stator to the engine block, or to bolt the stator to the outside of the dynamo, and put the rotor cup "upside down" against the crank.  I'll have to make an adapter to provide the seal to the front of the engine regardless.  The stator to the front makes it easier for the wires to come out to the terminal block on the dynamo casing.


The final part is the regulator / rectifier from a scooter.  I've bench-tested the rectifier / regulator up to 6 amps load.  It works fine with 14 vac input, and does not overheat.

Here's a VERY ROUGH sketch of the assembly.  I keep changing the design, so my dimensioned sketch is pretty bad.  I will require a minor modification to the dynamo case.  The cap screws will interfere with the side of case, so the case will need to be ground away in two small spots not visible from the outside.  The cap screws can be modified slightly to reduce the amount of grinding to the case.

Wednesday, April 6, 2011

MC45L Dynamo arrives

Just bought the proper dynamo for my S7 Deluxe.  The one that was on it was from a the earlier S7 model.  This one should have more current capability, since it has updated field coils, and four brushes instead of just two.  I knew it wouldn't include the bolts, so I probably will have to get those elsewhere... or use the ones that are on the bike.  It looks like its in fairly good shape for its age.



The commutator is a bit rough, but shows no signs of arcing.  It should be 100% functional.  The brush wires need routed, and the connector needs fastened down too, but it looks like its all there.  I may have to dress up the seal surface on the back of the rotor if I decide to use it. There's some pitting.  Its kinda a shame that the cover has been bead-blasted.  I would have preferred that it still had the original patina.  That's not to say that I couldn't GIVE it some patina.  Hmmm.

Hopefully, this all works and I can sell the older Lucas MC45O dynamo that's on the bike now to someone who needs it to make their original bike proper. (sold it!)

Saturday, February 26, 2011

New Seat Belts

I finally got tired of the single-sided retractable seat belts that were in my Imp when I bought it.  They kept retracting back behind the seats and you couldn't fasten your belt unless the door was open. If you let it loose, it would slam against the door pocket and disappear behind the seat.

I sent away for some new proper ones.  My friend Nick was kind enough to supply me with some Sunbeam stickers for the buckles.  They look pretty snappy!

Wednesday, January 19, 2011

Sunbeam S7 in the press

I was thumbing through the AMA magazine from September 1955, and I discovered a treasure. Here was an article reviewing the uniqueness of the S7 and then a page or so later a nearly full page advert.